车架式起落架减缩质量落震试验改进方法
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1南京航空航天大学航空学院,南京 210016;2南京航空航天大学机械结构力学及控制国家重点实验室,南京 210016;3南京航空航天大学飞行器先进设计技术国防重点学科实验室,南京 210016;4南京航空航天大学通用航空与飞行学院,溧阳 213300

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通讯作者:

魏小辉,教授,博士生导师,E-mail:wei_xiaohui@nuaa.edu.cn。

中图分类号:

V226

基金项目:

中央高校基本科研业务费专项基金(NS2024065)。


An Improved Reduced-Mass Method for Drop Test of Truck-Beam Landing Gears
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1College of Aerospace Engineering, Nanjing University of Aeronautics & Astronautics, Nanjing 210016, China;2State Key Laboratory of Mechanics and Control of Mechanical Structures,Nanjing University of Aeronautics & Astronautics, Nanjing 210016,China;3Key Laboratory of Fundamental Science for National Defense-Advanced Design Technology of Flight Vehicle,Nanjing University of Aeronautics & Astronautics,Nanjing 210016,China;4College of General Aviation and Flight, Nanjing University of Aeronautics & Astronautics, Liyang 213300, China

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    摘要:

    本文针对车架式起落架在传统减缩质量法落震试验中存在的吊篮垂向速度失真、导致动力学响应偏差的问题,以提高试验精度与工程适用性为目的,建立了车架式起落架多体动力学模型,对比分析了减缩质量法与升力加载法下的落震响应特性,揭示了传统方法因未模拟升力而导致触地后持续加速、速度超标的内在机理。通过提出一种基于参数反馈迭代的改进方法,对投放质量与高度进行联合优化调节,实现了速度与能量的协同等效。以某大型民机主起落架为研究对象进行仿真验证,结果表明:该方法将吊篮垂向速度误差从11.15%降低至0.13%,功量误差控制在2.34%以内,并使油液阻尼力峰值等关键载荷指标与升力加载法的差异缩小至4.01%。研究表明,所提出的改进方法在不引入复杂仿升系统的条件下,显著提升了车架式起落架落震试验的精度与可靠性,为起落架缓冲性能验证提供了一种高效工程解决方案。

    Abstract:

    Truck-beam landing gears usually face vertical velocity distortion of the drop test basket during traditional reduced-mass method drop tests, leading to deviations in dynamic response. Aiming to enhance test accuracy and engineering applicability, this study proposes a multibody dynamics model of the truck-beam landing gear. The drop response characteristics under both the reduced-mass method and the lift-loading method are compared and analyzed, revealing the inherent mechanism of the traditional method: The continuous post-touchdown acceleration and velocity overshoot due to the absence of lift simulation. An improved approach based on parameter feedback iteration is proposed, achieving simultaneous equivalence in velocity and energy through coordinated adjustment of the release mass and height. Simulation validation conducted on a main landing gear of a large civil aircraft demonstrates that the proposed method reduces the error in the basket’s vertical velocity from 11.15% to 0.13%, confines the energy error within 2.34%, and narrows the discrepancy in key load indicators (e.g., peak oil damping force) to 4.01% compared with the lift-loading method. The results indicate that the proposed method significantly enhances the accuracy and reliability of drop tests for truck-beam landing gears without introducing complex lift simulation systems, providing an efficient engineering solution for validating landing gear buffer performance.

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引用本文

李昕苒,魏小辉,房兴波,陈虎,刘中昊.车架式起落架减缩质量落震试验改进方法[J].南京航空航天大学学报,2026,58(3):598-605

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  • 收稿日期:2025-09-18
  • 最后修改日期:2026-01-08
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  • 在线发布日期: 2026-06-18
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